By
optimizing the roller press system and ball mill system, adjusting the position
of grinding aids, optimizing the dust into the process of selecting powder
machine, the output of cement grinding system is increased. Through the use of
air suspension fan, inverter fan transformation, elimination of high energy
consumption air compressor and other measures to upgrade the auxiliary equipment
to improve the efficiency of the fan and air compressor, the technological
process of grinding system was optimized by removing belt machine, skirt board
machine, spiral conveyor of dust collector, air chute of grinding tail dust
collector, reforming ash hopper and cyclone tube. It achieved the fine
management of grinding system due to reducing the idle and low-load operation
time of the equipment, reducing the compressed air leakage of the grinding
system, optimizing the spray frequency and piping arrangement of the dust
collectors, and using electricity to avoid peak-to-valley production and
operation. After transformation, the power consumption of cement preparation
section is reduced from 34.9 kW·h/t to 30.8 kW·h/t, which can meet the
requirement of national standard.